EFFECTIVENESS ANALYSIS OF GROUND IMPROVEMENT TREATED BY DYNAMIC CONSOLIDATION

동압밀공법을 이용한 지반개량 사례연구

  • 양정수 (현대엔지니어링 토목사업부) ;
  • 손준익 (한국건설기술연구원 지반 연구실 수석연구원)
  • Published : 1992.10.01

Abstract

This paper reports a case study of dynamic consolidation. The objective of the study is to evaluate the effectiveness of ground improvement at the site for Hyundai Petrochemical Compound constructed at Daesan-Myeon, Seosan-Gun in the western shores of Korea. The site ground was prepared by filling on the existing soft marine deposit which consists of a loose granular soil layer and a medium stiff clay layer. For the stabilization of site ground, the compaction was executed in three different procedures with same pounder weigh, drop height and imprint spacing. The post investigation showed that the object was successfully achieved indicating a significant increase of bearing capacity of the treated ground. In this study the effectiveness of dynamic consolidation is evluated for various factors the applied energy, temping sequences, the radial distance from the imprint location and the depth of bed rock.

Keywords